Originally Posted by labman
I may have made a big project out of a simple task yesterday, but at least I left things in much better shape than the last guy to work on it. It started the other day at church with a dripping faucet, maybe a Gerber washerless one. I paid $7 for a new cartridge at the hardware store. Afterwards I could only get a trickle of water out of either the hot or cold. The hot stop really didn't shut the water off completely, and the cold, the handle turned and turned either way and didn't do anything. Decided to come back yesterday afternoon when turning the main shutoff off would b less disruptive. Instead of angle stops, they were soldered in gate valves. Removed the guts and found the stem was twisted off and the gate gone. Work my way back to the wall unscrewing a 3/8 pipe to 3/8'' tubing adapter. I knew it was 3/8, because it said 3/8 on the old valve. Made a trip to the hardware store and picked up a 3/8 threaded ball valve, nipple, and street ell. Installed them giving me a nice stop for the cold, just needing connected to the copper tubing running to the faucet. I then took out the guts of the hot stop, scraped the lime off, and then discovered how easy it was to twist off the stem putting it back together. Looking a head a little before going to the hardware store again, I realized I would have to solder the tubing into the adapter with it already screwed into the valve. I was afraid I might melt the plastic seats in the valve, or not be able to get the valve back together without leaking. I decided my best bet was a pipe to compression adapter. Picked up two 3/8 to 3/8 ones along with another valve, nipple, and street ell. Got the hot stop done and was able to turn the main water valve on. I made sure the line was clean from the faucet back to the stops. Now, just make the compression to tubing joint, and it should be done. While studying the alignment and length, I discovered the 3/8 compression fitting was for 3/8 OD tubing, and the tubing was 3/8 ID. It was getting late, I had a meeting to go to. The more I thought about being pressed for time, the tubing not quite long enough, needing bent to align right, and having to put the compression fitting over the end tinned from the soldered joint, the less confident I was in the compression joint not leaking. Nuts with it. Since I had to make a third trip to the hardware store for the day, for $7 each, I picked up 4' lengths of the stainless steel braided flex, half inch pipe like the faucet one end and the same 3/8 compression fittings as I had at the other. This also eliminated a galvanized coupling between the brass faucet and the copper tubing adapter. Still couldn't get much water out until I cleaned the aerator.
The angle stops have their uses, but I can't see using the gate valves. The ball valves are much easier to use, and will shut the water off completely even after years of service in hard water.